Hi All,
Just this morning our KUKA KRC4 Palletising robot was stopped due to a fault on the safety interface board. It was not powering up.
So we replaced it with a new one. It is powering up perfectly but showing an error of SIB/SIB Extended Loopback contact error. Which is preventing the machine from running.
I am relatively new with this robot. Kindly guide me if i need to do any changes after replacement of the safety interface board?
I have attached a picture for your better understanding of the issue. Please help us out production is stopped due to it.