I'm operating, after playing with the MOC file I found my major problem was the wrong number of pole pairs. set to 2, it rotates just fine, now I have to just tweak the damper values.
Transmission ratio tripped me up for a bit, it was simply 90:1 (motor turns 90 degrees for table to turn 1 degree).
Here's my MOC file, operating mostly correctly, the only issue now is if I jog in a medium increment, it'll move, but then if I just sit there and keep holding the switch, it'll bump another notch. The degree changes correctly with it, so I think it'll be just fine.