Yeah we just replaced the E unit and now robot is now running. Thanks for all the tips guys. They were very helpful to find the problem
Posts by Ivan8793
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Will do, thanks for the tip
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Yes we did all of that. We check all fuses and everything and they all seem ok. So maybe we need to replace the E-Stop Board
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Hello there I'm currently using a M-20ia series robot and I'm stuck with this code Srvo-348 dcs mcc off alarm 01 and i called some people and they told me it was an E-stop Unit but we already checked them all and i cant find anything wrong with them. Any suggestions on what can i do next?
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I will check on that tomorrow when I'm back at work. And once again thanks for the help
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Thanks a lot guys
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Ok thanks I was just trying to make sure that the spindle doesn't get damaged because of it
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Will that help?
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Hello everyone so I have a robot that has a spindle that can go to 24,000 rpm to 40,000 but the people before me when programing they were setting up for the robot to only go to 1,500 to 1,800 rmp max. So my question is will it damage the spindle?
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Thanks I'm now requesting a diagram maybe it will help me
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We just replace a spindle today for a Fanuc and it wormed up and everything but now it shooting this message. Any help?
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Its now been fixed, one of the axis was off. When he mastered he didn't notice but today when we had the robot at position ZERO that's when we saw it. All we did was aligned it and re master and robot is back and running.
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He did and I guess he coming back tomorrow to fix the mess. I'll get back with you guys and see what he did wrong just in case someone else has the same issue. Thanks for the help even tho I couldn't do much but it's appreciated
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Thanks for all the info guys. I'll do my best to make this run again.
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I already try that and still the same.
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I think the mastering was wrong because even tho I try to touch up my 3 points again (origin, x and y) still off by 20 or even more mm. And I'm not sure where to go from here. A professional came and did the job but I wasn't here so I'm not sure what he did wrong and I'm stuck here
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I'm off like 20mm
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This is what I get, and like I said I been using u frames when I program something new and now everything is way off since they came and remaster the robot. I'm including a picture of a fixture showing how off my program is
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Does anyone know how to do u frames recovery for fanuc robots? I recently had a guy remaster 2 robots here and one fix but the other one everything shifter about 10mm from where it used to be and I don't know how to re teach u frames