issue fixed.
Dual change signal, made x10.5 and x10.6 on/off at the same time. got synchronized.
not synchronized reason for my case is that I get 10.5 to (GND) and then turn on/off 10.6 to +24V, not at the same time.
issue fixed.
Dual change signal, made x10.5 and x10.6 on/off at the same time. got synchronized.
not synchronized reason for my case is that I get 10.5 to (GND) and then turn on/off 10.6 to +24V, not at the same time.
Hi Enagy, issues fixed? would you please to share how.
Thank you Srtautomation for sharing.
I am have the same issue with the robot ABB Robot IRB6640 M2004 which stuck on "SC1 not synchronized" fault.
* About "Found the Servo Motors were not synchronized- Clicked on Synchronize motors." posted above, can you share more details? where can find motors that are not synchronized.
* Tried to synchronize with Robostudio 2020 under safemove menu , read joints values from controller, joint 1,4,5,and 6 are 0.0, joint 2 =-0.6, joint 3=-0.5. it was not able to move the robot before clean the fault, I set these values to synchronize and write to controller. it was not work. will try all 0 tomorrow.