Thanks for everybody for the help, but the robot still not move
Somebody have idea what can I do with this robot to move?
Please help!!!!
Thanks for everybody for the help, but the robot still not move
Somebody have idea what can I do with this robot to move?
Please help!!!!
This was, what I do first , some weeks ago. In that time was Dterr in all axes.
Now in group 2, 3 have error in startup, and it can be erase, after when I enable the output in test cycle Menu 2.
What I need to do with Dterr.
If can be erase is it real error?
This have until, when the motion data output changed to enable.
Maybe the motion data output is wrong?
This message come up when restart.
Ist can be erase, and after no alarm message
Here some photos of the TP screen
When star up got other message srvo-068
After in menu 2 digital output need to change to enable and break off, after fails can erase. If erase the alarm messages, no active alarms.
Where can see the over ride speed?
Firstly the battery replaced and after got some errors.
Now only the srvo-075 left. No any active alarm.
If push shift-reset after have PRIO-063 Rack0 slot1
If push again the shift this disappear and SRVO-075 show .
I pressed the RES_PCA and after turn off /on the robot but nothing changed. Cycle power is off-on the robot?
Can't move any arm.
If I push SHIFT and any Jx , get a noise in the arm, like relay or break switch on or off, and electircal noise in 30 sec and after turn of.
Manually cant turn the robot in this time.
Maybe the break not released.
I don't know, how can be release the break or turn the arms manually in position.
We have another robot, what have manual switch and after I can turn the arms manually.
You cannot master the robot until the SRVO-075 alarm is cleared on each axis.
Somebody have idea what I need to do for move any axis?
Hi
I have same problem. Battery dead. Replaced, bal, srvo-075, not move , not mastered
Any other idea, how to solve?
Thax for the help in the other topic but still I have this problem
I opened the TP, repaired the missing lines.
Without shift push the J1-Jx buttons wrote "push shift key" in the top line.
The shift is OK.
I thing, something parameter is wrong somewhere, but I don't know what and where.
Hi
Now in joint mode the TP
I can't change it when I push the coord. I don't know why.
When I push the Shift and after any axe can hear an noise from the servo, like something switch on, or off, or relay turn on/off.
And can hear electric noise like a motor try to start.
This until 30 sec hold and switch off.
The SRVO-075 G1 A6 always can see in the top line.
If I push the reset can see
If push shift-reset after have PRIO-063 Rack0 slot1
If push again this disappear and SRVO-075 show .
Not mastered
Somebody have any idea?
Hi
We have an Fanuc robot with R-J3
This robot not used long time ago and battery need to replace. After have a lot of errors what is solved here. Many thanks for it.
Actual error message SRVO-075 G:1 A:6
Somebody have any idea what can I do with it?
I tried to remaster but finally the $MASTER_DONE can't change to DONE always change back to FALSE in a second
Hi
Our company have an VRS 1-1 whan not worked at least in 5 years ago.
I turned on in yesterday an firstly the date need to set, and after showed hhd missing or need reformat.
Somebody can help what I need to do, or manual can put somewhere to donwload me.
Good question. I don't remember now.
Tomorrow will check in the TP, maybe will remember.
I try to modify the things and now i have mctl-003 error and prio-063
Yes it is true.
Maybe some parameter is not correct. I not have idea, what is wrong.
The TP can't change, I have only this
Because the battery was dead, the robot forget the thing and need recabrating, but when I try remastering/ calibrating it is not done reply not calibrated, not mastered.
And still can't move any arm after joint it
How to rotate the arm? Not move any axe This was the basic problem.
Now I can read the top line
SRVO-075 Pulse not established(G:1 A:6)
The shift key is ok.
In the top line have message srvo something, but cant read it